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Old Jul 27, 2004 | 08:18 PM
  #5  
k.a.y's Avatar
k.a.y
Senior Member
 
Joined: Jul 2002
Posts: 472
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From: Hailey, Idaho
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Actually, I fixed it. My idle adjustment screw was too loose, AND I had a faulty TB gasket. Also, my main reason to do the coolant bypass/iac mod was that my iacv was screwed up to begin with. But if I wanted to, i have the vlave off my other motor to throw on there if something in the mod acts up. Runs prefect for right now, though.
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